Status operasional unit pembangkit
Kapasitas daya yang tersedia
Nama Unit | Mesin | DMN | DMP | Beban | Status | Progres | Waktu Update |
---|---|---|---|---|---|---|---|
PLTU MORAMO ( Subsistem Kendari ) | MORAMO #1 | 50.0 | 50.0 | 47.5 MW | β‘ Operasi |
|
01/08/2025 09:22:56 |
PLTU MORAMO ( Subsistem Kendari ) | MORAMO #2 | 50.0 | 50.0 | 47.5 MW | β‘ Operasi |
|
01/08/2025 09:22:56 |
PLTD Wua Wua | MAK #1 | 1.7 | 1.7 | 0.0 MW | π Standby |
|
31/07/2025 08:26:04 |
PLTD Wua Wua | MAK #2 | 1.6 | 1.6 | 0.0 MW | π Standby |
|
31/07/2025 08:26:04 |
PLTD Wua Wua | MAK #3 | 1.7 | 1.7 | 0.0 MW | π Standby |
|
31/07/2025 08:26:04 |
PLTD Wua Wua | Mak #4 | 1.7 | 1.7 | 0.0 MW | π Standby |
|
31/07/2025 08:26:04 |
PLTD Wua Wua | MAK #5 | 1.3 | 1.0 | 0.0 MW | π Standby |
|
31/07/2025 08:26:04 |
PLTD Poasia | MIRR #1 | 1.7 | 1.4 | 0.0 MW | π Standby |
|
01/08/2025 08:46:00 |
PLTD Poasia | MIRR #2 | 0.0 | 1.4 | 0.0 MW | π§ Pemeliharaan |
|
01/08/2025 08:46:00 |
PLTD Poasia | MIRR #4 | 0.0 | 0.0 | 0.0 MW | β οΈ Gangguan |
|
01/08/2025 08:46:00 |
PLTD Poasia | MIRR #5 | 1.7 | 1.4 | 0.0 MW | π Standby |
|
01/08/2025 08:46:00 |
PLTD Poasia Containerized | CUMS #1 | 1.0 | 0.9 | 0.0 MW | π Standby |
|
01/08/2025 08:46:00 |
PLTD Poasia Containerized | CUMS #2 | 1.0 | 0.9 | 0.0 MW | π Standby |
|
01/08/2025 08:46:00 |
PLTD Poasia Containerized | CUMS #3 | 1.0 | 0.9 | 0.0 MW | π Standby |
|
01/08/2025 08:46:00 |
PLTD Kolaka | DHS #1 | 0.4 | 0.4 | 0.0 MW | π Standby |
|
30/07/2025 09:11:45 |
PLTD Kolaka | DHS #2 | 0.4 | 0.4 | 0.0 MW | π Standby |
|
30/07/2025 09:11:45 |
PLTD Kolaka | DHS #3 | 0.3 | 0.3 | 0.0 MW | π Standby |
|
30/07/2025 09:11:45 |
PLTD Kolaka | NIGATA #3 | 0.3 | 0.5 | 0.0 MW | π Standby |
|
30/07/2025 09:11:45 |
PLTD Kolaka | MAK #1 | 1.8 | 1.8 | 0.0 MW | π Standby |
|
30/07/2025 09:11:45 |
PLTD Kolaka | MAK #2 | 1.8 | 1.8 | 0.0 MW | π Standby |
|
30/07/2025 09:11:45 |
PLTD Lanipa Nipa | DEUTZ BV #2 | 0.7 | 0.7 | 0.0 MW | π Standby |
|
30/07/2025 09:11:45 |
PLTD Lanipa Nipa | DEUTZ BV #3 | 0.7 | 0.0 | 0.0 MW | π Standby |
|
30/07/2025 09:11:45 |
PLTD Lanipa Nipa | DEUTZ BV #4 | 0.8 | 0.8 | 0.0 MW | π Standby |
|
30/07/2025 09:11:45 |
PLTD Lanipa Nipa | MAN #1 | 0.4 | 0.4 | 0.0 MW | π Standby |
|
30/07/2025 09:11:45 |
PLTD Ladumpi | YANMAR #1 | 0.2 | 0.2 | 0.0 MW | π Standby |
|
30/07/2025 09:11:45 |
PLTD Ladumpi | YANMAR #2 | 0.2 | 0.2 | 0.0 MW | π Standby |
|
30/07/2025 09:11:45 |
PLTD Ladumpi | CUMS #2 | 0.0 | 0.0 | 0.0 MW | π Standby |
|
30/07/2025 09:11:45 |
PLTM Sabilambo | ZJG #1 | 1.0 | 1.0 | 1.0 MW | β‘ Operasi |
|
30/07/2025 09:11:45 |
PLTM Sabilambo | ZJG #2 | 1.0 | 1.0 | 1.0 MW | β‘ Operasi |
|
30/07/2025 09:11:45 |
PLTM Mikuasi | MIKUASI #1 | 0.5 | 0.5 | 0.5 MW | β‘ Operasi |
|
30/07/2025 09:11:45 |
PLTD Bau Bau | DHS #3 | 0.8 | 0.5 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTD Bau Bau | DHS #4 | 0.8 | 0.5 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTD Bau Bau | DEUTZ BV #1 | 0.8 | 0.7 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTD Bau Bau | DEUTZ BV #2 | 0.7 | 0.6 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTD Bau Bau | DEUTZ BV #3 | 0.7 | 0.5 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTD Pasarwajo | CUMS #1 | 0.0 | 0.9 | 0.0 MW | π§ Pemeliharaan |
25 July 2025
- Rencana akan dilakukan pengujian engine
- dari hasil pengujian terahir FSNL( senin 7 July 2025) di temukan anomali pada 1 core fasa V winding stator generator
- tindak lanjutnya perbaikan dan pemeriksaan oleh tim CBM dan mesindo
1. Pengecekan generator kendala temuan short stator gen pasca
direwinding (21 Feb 25)
2. Pengukuran nilai tahanan generator (21 Feb 25)
3. Klaim garansi dan Pembongkaran generator (28 Feb 25)
4. Pengiriman generator ke workshop (6 Mar 25)
5. Rewinding generator (20 Mar 25)
6. Pengetesan generator (11 Jun 25)
7. Mobilisasi generator dari workshop (13 Jun 25-4 Jul 25)
8. Instal generator (13 Jul 25)
9. Running test (13 Jul 25) kendala salah satu phasa S temp kabel power abnormal, sementara dilakukan pemeriksaan lanjutan oleh pihak pelaksana rewinding gen.
Kendala
Rabu 09 Juli 2025
Realisasi (90 %)
Rencana Selanjutnya :
- Menunggu tindak lanjut dari pihak pelaksana estimasi on site hari jumat 11 July
Realisasi 8 July 2025 :
- Pengecekan wiring
- Pengecangan baut cover housing bearing fan radiator
- Final check
- Running test idle dan rated (FSNL)
- Pengujian phasa squence
- uji emergency Stop
- Temuan satu core temperature abnormal fasa V (menunggu konfirmasi pelaksana minggu 3 Jul 25)
|
31/07/2025 08:43:48 |
PLTD Pasarwajo | CUMS #2 | 1.0 | 0.9 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTM Winning | BWTR #1 | 0.8 | 0.0 | 0.7 MW | β‘ Operasi |
|
31/07/2025 08:43:48 |
PLTM Winning | BWTR #2 | 0.8 | 0.8 | 0.8 MW | β‘ Operasi |
|
31/07/2025 08:43:48 |
PLTD Raha | DHS #3 | 0.4 | 0.4 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTD Raha | MIRR | 1.8 | 1.6 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTD Raha | DEUTZ BV #1 | 0.0 | 0.6 | 0.0 MW | β οΈ Gangguan |
29 Juli 2025
realisasi (60 %)
- progres saat ini waiting material pemulihan (Est. M2 Agustus 2025)
"1. Pengecekan exhaust manifold sisi turbocharger (16 Okt 24)
2. Pengecekan cylinder head no.3 dan 8 (16 Okt 24)
3. Pembongkaran turbocharger (16 Okt 24)
4. Pembongkaran cylinder head no.3 dan 8 (16 Okt 24)
5. Inventarisasi kebutuhan material pemulihan (17 Okt 24)
6. Pengadaan Material (Proses Levering Material, paralel menunggu PJ terbit)
7. Penggantian innert part dan Rekondisi turbocharger (22 Mei 25)
8. Pengiriman turbocharger ke Site (13 Juni 25) " SELESAI " TERPASANG
9. Proses levering material korektif pemulihan, kendala material tertahan dibea cukai (est tiba di site M1 Agustus 2025)
10. Running Test (est M2 Ags 2025)"
|
31/07/2025 08:43:48 |
PLTD Raha | CUMS #1 | 0.8 | 0.9 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTD Raha | CUMS #2 | 0.8 | 1.0 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTD Raha | CUMS #3 | 0.0 | 0.8 | 0.0 MW | β Overhaul |
|
31/07/2025 08:43:48 |
PLTD Raha | CUMS #4 | 0.8 | 0.9 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTD Raha | CUMS #5 | 0.0 | 0.9 | 0.0 MW | β οΈ Gangguan |
1. Pengecekan axial conrod semua cyl (finish)
2. Pembongkaran Conrod Cyl No.2A dan No.2B (finish)
3. Pembersihan crankpin journal No.2 (finish)
4. Polishing crankpin journal No.2 (finish)
5. Assessment crankshaft bidang Enj UP (hasil spot check ditemukan crack)
6. Terdapat opsi pemanfaatan equipment dari PLTD Gunung Sitoli mesin KTA 50 G3 yang berstatus ATTB, perlu dikaji lebih lanjut relokasi material internal UP (sudah bersurat ke Ditgas terkait kajian pemanfaatan material tgl 1 Nov 24)
7. Assessment oleh PT ALTRAK (hasil masih layak untuk 1 unit complete dan 1 unit sudah tidak complete namun crankshaft masih layak pakai) 30-Jul-24
8. Relokasi Material dari PLTD Gunung Sitoli (est. pembongkaran di site PLTD Gunung Sitoli M3 Juni, dengan esti. material tersebut tiba di site pada M2 Juli 2025)
9. Kontrak khs overhaul sudah terbit DO , rencana dibarengkan pelaksanaan Final Stage (21 Mar 25)
10. Proses penyusunan kebutuhan material pemulihan diluar scope OH ( Sementara Proses tender Estimasi terkontrak M3 Agustus, levering Mat. M3 Okt sampai di site)
11. Generator diambil atasi ggn unit 4 (Nodis ke ICC tgl. 17 Mar 25 pembuatan HPE)
- Dokumen laksdan ( update persiapan tender )
12. Instal material pemulihan (est M4 Okt 25)
13. Running Test (est M4 Nov 25)
|
31/07/2025 08:43:48 |
PLTD Raha | MITS #1 | 0.0 | 1.0 | 0.0 MW | β Overhaul |
|
31/07/2025 08:43:48 |
PLTD Raha | MITS #2 | 0.0 | 0.0 | 0.0 MW | β οΈ Gangguan |
1. sudah bersurat ke UP Kendari Tanggal 18 November 2024, penyampain gangguan, laporan investigasi, BA. Material terpakai di unit lain dan List material kebutuhan pemulihan mesin tersebut. (material sdh banyak di manfaatkan ke unit lain)
2. Rewinding generator ex-wangi - wangi 28 Feb 25
3. Rewinding Trafo ex-wangi - wangi (proses packing) est. M2 Mar 25
4. Perlu dikaji lebih lanjut oleh internal UP terkait opsi RU krn secara fisik sdh, equipment sdh banyak pindah
5. Nota Dinas Har ke Enj (8-Okt-24)
6. Update kembali Inventarisasi kebutuhan material pemulihan dengan mengoptimalisasi material eks overhaul (Permintaan PH)
7. Proses pencarian kembali mesin yang dapat dimanfaatkan ( Estimasi M4 Agustus 2025 )
8. Rencana Masuk sistem ( M4 Desember )
|
31/07/2025 08:43:48 |
PLTD Raha | MITS #4 | 0.7 | 0.8 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTD Raha | MITS #3 | 0.0 | 0.0 | 0.0 MW | β οΈ Gangguan |
1. Pemeriksaan Axial Conrod (27 Des 22)
2. Pembongkaran Conrod Cyl No.5 (27 Des 22)
3. Pembersihan crankpin journal No.5 (27 Des 22)
4. Polishing crankpin journal No.5 (27 Des 22)
5. Klaim Garansi ke pihak pelaksana terkait Crankshaft (selesai)
6. Pengiriman crankshaft pengganti dan sebagian material pemulihan dari pihak pelaksana (belum ada kesepakatan antara pelaksana dengan pemilik crankshaft)
7. Rewinding Generator sudah tiba (28 Feb 25)
8. Perbaikan Block Engine di workshop (28 Jan 25)
9. Kesepakatan Pelaksanaan Jasa untuk permulihan (selesai)
10. Dokumen Rencana Pengadaan material korektif pemulihan sudah turun ke ICC (10 Juni 2025) dengan levering material 45-60 hari setelah PJ terbit
Update :
Dokumen persiapan tender di pelksana pengadaan ( Estimasi terkontrak M3 Agustus, estimasi levering material tiba on site M3 Okt )
11. Tim ITI akan tiba disite est M1 Jul 25 (Menunggu Realisasi hingga deadline 31 Juli 2025 , jika tidak ada tindak lanjut akan dilakukan suakelola sambil menunggu levering material )
12. Running Test est M1 November 25
|
31/07/2025 08:43:48 |
PLTD WANGI-WANGI ( SIstem Isolated Wangi-Wangi ) | DHS #1 | 0.4 | 0.2 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTD WANGI-WANGI ( SIstem Isolated Wangi-Wangi ) | DHS #2 | 0.3 | 0.1 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTD WANGI-WANGI ( SIstem Isolated Wangi-Wangi ) | SWD #1 | 0.3 | 0.2 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTD WANGI-WANGI ( SIstem Isolated Wangi-Wangi ) | SWD #2 | 0.3 | 0.2 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTD WANGI-WANGI ( SIstem Isolated Wangi-Wangi ) | SWD #3 | 0.2 | 0.0 | 0.0 MW | π Standby |
|
31/07/2025 08:43:49 |
PLTD WANGI-WANGI ( SIstem Isolated Wangi-Wangi ) | CUMS 1 | 0.9 | 0.8 | 0.0 MW | π Standby |
|
31/07/2025 08:43:49 |
PLTD WANGI-WANGI ( SIstem Isolated Wangi-Wangi ) | CUMS 2 | 1.0 | 0.9 | 0.7 MW | β‘ Operasi |
|
31/07/2025 08:43:49 |
PLTD WANGI-WANGI ( SIstem Isolated Wangi-Wangi ) | MITS #1 | 1.0 | 0.8 | 0.7 MW | β‘ Operasi |
|
31/07/2025 08:43:49 |
PLTD WANGI-WANGI ( SIstem Isolated Wangi-Wangi ) | MITS #2 | 1.0 | 0.0 | 0.7 MW | β‘ Operasi |
|
31/07/2025 08:43:49 |
PLTD WANGI-WANGI ( SIstem Isolated Wangi-Wangi ) | MITS #3 | 1.0 | 0.5 | 0.6 MW | β‘ Operasi |
|
31/07/2025 08:43:49 |
PLTD WANGI-WANGI ( SIstem Isolated Wangi-Wangi ) | MITS #4 | 0.0 | 0.9 | 0.0 MW | π§ Pemeliharaan |
|
31/07/2025 08:43:49 |
PLTD WANGI-WANGI ( SIstem Isolated Wangi-Wangi ) | MITS #5 | 0.0 | 0.0 | 0.0 MW | β οΈ Gangguan |
- Pembongkaran exciter (14 Jul 25)
- Pengecekan stator exciter (14 Jul 25)
- pengiriman exciter (16 Jul 25)
- rewinding exciter (est. 17 Jul 25)
- Install exciter (est. 20 Jul 25)
- Running test (est. 20 Jul 25)
|
31/07/2025 08:43:49 |
PLTD WANGI-WANGI ( SIstem Isolated Wangi-Wangi ) | MITS #6 | 1.0 | 0.7 | 0.6 MW | β‘ Operasi |
|
31/07/2025 08:43:49 |
PLTD LANGARA ( Isolated SistemΒ LangaraΒ ) | CUMS #1 | 0.5 | 0.5 | 0.3 MW | π Standby |
|
31/07/2025 08:26:04 |
PLTD LANGARA ( Isolated SistemΒ LangaraΒ ) | CUMS #2 | 0.5 | 0.5 | 0.3 MW | π Standby |
|
31/07/2025 08:26:04 |
PLTD LANGARA ( Isolated SistemΒ LangaraΒ ) | CAT | 0.2 | 0.1 | 0.0 MW | π Standby |
|
31/07/2025 08:26:04 |
PLTD LANGARA ( Isolated SistemΒ LangaraΒ ) | MAN #1 | 0.3 | 0.3 | 0.0 MW | π Standby |
|
31/07/2025 08:26:04 |
PLTD LANGARA ( Isolated SistemΒ LangaraΒ ) | MAN #2 | 0.4 | 0.3 | 0.0 MW | π Standby |
|
31/07/2025 08:26:04 |
PLTD LANGARA ( Isolated SistemΒ LangaraΒ ) | MITS #1 | 1.0 | 1.0 | 0.9 MW | π Standby |
|
31/07/2025 08:26:04 |
PLTD LANGARA ( Isolated SistemΒ LangaraΒ ) | MITS #2 | 0.0 | 1.0 | 0.0 MW | β Overhaul |
|
31/07/2025 08:26:04 |
PLTD EREKE ( Sistem Isolated Ereke ) | DHS #3 | 0.4 | 0.3 | 0.0 MW | π Standby |
|
31/07/2025 08:43:49 |
PLTD EREKE ( Sistem Isolated Ereke ) | DHS #6 | 0.2 | 0.2 | 0.0 MW | π Standby |
|
31/07/2025 08:43:49 |
PLTD EREKE ( Sistem Isolated Ereke ) | DHS #7 | 0.4 | 0.4 | 0.0 MW | π Standby |
|
31/07/2025 08:43:49 |
PLTD EREKE ( Sistem Isolated Ereke ) | DHS #9 | 0.3 | 0.3 | 0.0 MW | π Standby |
|
31/07/2025 08:43:49 |
PLTD EREKE ( Sistem Isolated Ereke ) | CUMS #1 | 0.9 | 0.9 | 0.7 MW | β‘ Operasi |
|
31/07/2025 08:43:49 |
PLTD EREKE ( Sistem Isolated Ereke ) | CUMS #2 | 0.4 | 0.0 | 0.0 MW | π Standby |
|
31/07/2025 08:43:49 |
PLTD EREKE ( Sistem Isolated Ereke ) | CUMS #3 | 1.0 | 1.0 | 0.8 MW | β‘ Operasi |
|
31/07/2025 08:43:49 |
PLTMG KENDARI ( Subsistem Kendari ) | WARTSILA #1 | 8.0 | 9.8 | 0.0 MW | π Standby |
|
01/08/2025 09:22:56 |
PLTMG KENDARI ( Subsistem Kendari ) | WARTSILA #2 | 8.0 | 9.8 | 6.0 MW | β‘ Operasi |
|
01/08/2025 09:22:56 |
PLTMG KENDARI ( Subsistem Kendari ) | WARTSILA #3 | 8.0 | 9.8 | 0.0 MW | π Standby |
|
01/08/2025 09:22:56 |
PLTMG KENDARI ( Subsistem Kendari ) | WARTSILA #4 | 8.0 | 9.8 | 0.0 MW | π Standby |
|
01/08/2025 09:22:56 |
PLTMG KENDARI ( Subsistem Kendari ) | WARTSILA #5 | 8.0 | 9.8 | 0.0 MW | π Standby |
|
01/08/2025 09:22:56 |
PLTMG KENDARI ( Subsistem Kendari ) | WARTSILA #6 | 8.0 | 9.8 | 6.0 MW | β‘ Operasi |
|
01/08/2025 09:22:56 |
PLTU BARUTA ( Sistem Bau-Bau ) | BARUTA #1 | 6.0 | 6.0 | 5.5 MW | β‘ Operasi |
|
01/08/2025 09:22:56 |
PLTU BARUTA ( Sistem Bau-Bau ) | BARUTA #2 | 6.0 | 6.0 | 5.5 MW | β‘ Operasi |
|
01/08/2025 09:22:56 |
PLTMG BAU-BAU ( Sistem Bau-Bau ) | UNIT #1 | 9.8 | 9.8 | 6.3 MW | β‘ Operasi |
|
01/08/2025 09:22:56 |
PLTMG BAU-BAU ( Sistem Bau-Bau ) | UNIT #2 | 9.8 | 9.8 | 6.3 MW | β‘ Operasi |
|
01/08/2025 09:22:56 |
PLTMG BAU-BAU ( Sistem Bau-Bau ) | UNIT #3 | 9.8 | 9.8 | 6.3 MW | β‘ Operasi |
|
01/08/2025 09:22:56 |
PLTMG BAU-BAU ( Sistem Bau-Bau ) | UNIT #4 | 9.8 | 9.8 | 6.3 MW | β‘ Operasi |
|
01/08/2025 09:22:56 |
PLTM RONGI | UNIT #1 | 0.4 | 0.4 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
PLTM RONGI | UNIT #2 | 0.4 | 0.4 | 0.0 MW | π Standby |
|
31/07/2025 08:43:48 |
No | Tanggal | Unit | Agenda | Pimpinan Rapat | Aksi |
---|---|---|---|---|---|
1 | 28/07/2025 | UPKD | Daily Meeting 28 Juli 2025 | Asman Pemeliharaan | |
2 | 24/07/2025 | UPKD | Pembahasan Teknis Rencana Pemulihan Bendungan PLTM... | Manager UP Kendari | |
3 | 24/07/2025 | UPKD | Daily Meeting 24 Juli 2025 | Asman Pemeliharaan | |
4 | 22/07/2025 | UPKD | Notulen rapat Daily Meeting | Asman Pemeliharaan | |
5 | 21/07/2025 | UPKD | Daily Meeting 21 Juli 2025 | Muh. Amrullah | |
6 | 20/07/2025 | UPKD | admin | admin |
Lihat
4
|
7 | 16/07/2025 | UPKD | admin | admin |
Lihat
4
|
8 | 15/07/2025 | UPKD | Rapat Pembahasan Tindaklanjut Kontrak KDB022.PJ/61... | Abdul Rahman |
Lihat
24
|
9 | 14/07/2025 | UPKD | Pembahasan Hasil Site Visit Dan Assessment Kondisi... | Wigung Tri | |
10 | 14/07/2025 | UPKD | Udangan Rapat Pembahasan Progres Pekerjaan KDB158.... | Muh. Amrullah |